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Case
Studies
Case
Study 8 –
Fraud Investigation on Logistics and Distribution Centre
Industry:
Oil and Gas Refining and Distribution (Indian Ocean).
Client:
Private limited company.
Objective:
To identify the source of logistics losses ex- logistics
centre.
Results:
The company had won the competitive bids during privatization
of government assets on the island nation in the Indian Ocean
in 2000. Their assets included a refinery on the coast and
roughly 25% of the distribution network that was formerly
owned by a government state owned company.
The
directors and shareholders of the company suspected something
was amiss with the annual losses on throughput/ transport
of petroleum products from the logistics and storage facility
to the distribution points. These were much higher than the
industry average. The Internal Audit Director was asked to
investigate.
During
a major cyclone in the early 1990's much of the island's infrastructure
had been damaged and was inoperative. This included the rail
system which used to transport the petroleum products to the
capital of the country. As a result transportation by road
had commenced and grown rapidly, using old petroleum trucks
imported from Europe, often of a sub standard nature and quality.
The business was controlled mostly by a specific ethnic group
whose family connections had assisted with the rapid development
of road transport and logistics services.
The
logistics centre from where trucks would collect the product
for transportation was in a fairly bad state, due to effects
from cyclones as well as continuous under investment over
the years. As a result, there were no weigh bridges in operation
to weigh the before and after loading weight of trucks. Similarly,
no meters had been installed at the dispensing gantries to
measure the quantity of product loaded. Instead, a system
of calibration certificates was used, whereby each truck would
be calibrated and a certificate officially issued by the state
calibration authorities.
The
process was that a truck would arrive at the Logistics center,
a dip would be taken to ascertain whether the truck was fully
empty, the truck would be filled and then a dip would be taken
to ascertain the level of product in the compartments. Using
the calibration certificates the volume of product in the
truck would be calculated and noted on a delivery slip. At
the other end of the trip in the capital, the calibration
certificate would be produced for discharging and a similar
calculation would be made to calculate the total off load,
which would then be compared with a copy of the delivery note
to work out the losses. These losses would then be apportioned
to the four distribution companies on a pro rata basis.
In theory this sounded like the best option considering the
absence of weigh stations and meters on load points and considering
the calibration certificates were issued by a government calibration
department and maintained on a two yearly basis when each
truck had to be re calibrated independently.
The
investigation was undertaken by observation, reviewing records
including calibration certificates and interview with people
involved with the transportation and logistics process. Fortunately,
at a certain point in time both the logistics centre and the
distribution facility had started to take copies of calibration
certificates to put on file for each truck.
At the same time there were several reports of petroleum products
being sold on the road from the logistics centre to distribution
points in jerry cans at below market prices; A few police
officers also visited me and reported on first hand observations
of such practices.
As a result of on going investigations I finally found the
cause of the losses. It became evident that many truck drivers
had in fact two versions of calibration certificates with
differences of up to 1,000 liters of product at the calibrated
levels on the certificate. They would present one version
with a higher level at the logistics centre and the second
with a lower overall volume at the delivery point. They would
siphon off the differences en route, by breaking the lead
seals on the manhole covers on top of the truck, and then
replace the seals themselves with counterfeit or original
seals obtained on the black market. Another option often utilized
was the use of an overflow pipe in one of the compartments
which would be connected directly to the truck fuel compartment
and would hence provide the trucks free fuel. Discussions
with previous employees of the state owned company identified
this practice had been going on since the early days when
raid transport replaced rail transport after the damage caused
by the cyclone.
I
completed full calculations and obtained evidence going back
years, including identifying the issuing agency for the fake
calibration certificates and subsequently met with the truck
company owners to recover losses going back up to 3 years.
Most of these companies settled and some went into liquidation
as a result. Other results of this investigation were:
Improved
physical controls. The company commenced installing flow
meters at loading bays at the Logistics centre and also invested
in a weighbridge.
Improved
site security. A new firm of security guards was engaged
with specific scope of work to conduct gate checks on a random
basis.
Introduction
of new policies and procedures for logistics. I wrote
and introduced a new set of policies and procedures to formally
confirm requirements for the Logistics centre staff to observe
loading and dispatch controls.
About
USD 500,000 was recovered as a result of the 1 year long investigation
and subsequent negotiations.
Lesson
learnt:
Collusion can defeat even the best internal controls.
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